HELP! Horrible idle after plug swap.
#1
HELP! Horrible idle after plug swap.
Truck had a slight rough idle and 122k on original plugs. I did a plug change to the SP-534 and gapped about .030-.031. The plugs I removed were in the .50s! I am wondering now if the piece I used to gap is correct. I used small amount of anti-seeze but no where near the electrode part as I know that can cause issues. Used a small amount of di-electric grease inside the boot and wiped off them off. What I found is when the truck warms up its buttery smooth idle. First start after plugs it took 2 min and it was smooth. Drove all day. Started i this morning and it was real rough. Took over 10 min for it to go away and what I noticed is it took forever for the truck to warm up. Stayed on the cold side and didn't move off it for a good 10+ min.. when it got into normal operating temp range issue gone.. truck idled so smooth I could not even tell it was running!.. I just bought this truck and wife is on me about the issues... I appreciate any and all Help.. I am going to do an computer reset when I get home tonight. I assume this needs to be done when the truck is 100% cold? I have also heard there is a flash update for the computer as well?
#2
Senior Member
Year model and engine will probably help us help you.
#3
So Sorry.. 2011 Ford Ecoboost FX2 4door.
I did clean the motor during the spark plug change which had me worried i got something wet I should not have. Also the truck does have an airaid cold air intake on it. No tune and original owner ran it on 87 its whole life. I am starting to wonder if I knocked off a vacuum line during plug swap. It's a super rough idle. Watching it take forever to warm up was kinda odd as well. This is all real stressful since it took a week to convince the wife we needed this truck just to end up having issues to fix including the slip yoke bump..
I did clean the motor during the spark plug change which had me worried i got something wet I should not have. Also the truck does have an airaid cold air intake on it. No tune and original owner ran it on 87 its whole life. I am starting to wonder if I knocked off a vacuum line during plug swap. It's a super rough idle. Watching it take forever to warm up was kinda odd as well. This is all real stressful since it took a week to convince the wife we needed this truck just to end up having issues to fix including the slip yoke bump..
#4
Senior Member
So Sorry.. 2011 Ford Ecoboost FX2 4door.
I did clean the motor during the spark plug change which had me worried i got something wet I should not have. Also the truck does have an airaid cold air intake on it. No tune and original owner ran it on 87 its whole life. I am starting to wonder if I knocked off a vacuum line during plug swap. It's a super rough idle. Watching it take forever to warm up was kinda odd as well. This is all real stressful since it took a week to convince the wife we needed this truck just to end up having issues to fix including the slip yoke bump..
I did clean the motor during the spark plug change which had me worried i got something wet I should not have. Also the truck does have an airaid cold air intake on it. No tune and original owner ran it on 87 its whole life. I am starting to wonder if I knocked off a vacuum line during plug swap. It's a super rough idle. Watching it take forever to warm up was kinda odd as well. This is all real stressful since it took a week to convince the wife we needed this truck just to end up having issues to fix including the slip yoke bump..
#5
Thank you. Wife stressing thinking trans is going out lol. We aren't made out of money and this truck was smoking good deal because I got it off a friend. I will attempt that fix tonight on the slip yoke. The next thing to resolve is this horrible idle. So strange how after 10 min of driving its so smooth I have to look at the tach to see if its even running... its literally that smooth. Been around cars my whole life and drag raced for 20 years. When I mean Smooth I mean its extremely smooth when warmed up. Like I said tho.. I am starting to question my spark plug gauge for gapping. The factory were all over .050.. if its off then its possible it could be gapped super low. its a tiny gap i know that much.
#6
Senior Member
Thank you. Wife stressing thinking trans is going out lol. We aren't made out of money and this truck was smoking good deal because I got it off a friend. I will attempt that fix tonight on the slip yoke. The next thing to resolve is this horrible idle. So strange how after 10 min of driving its so smooth I have to look at the tach to see if its even running... its literally that smooth. Been around cars my whole life and drag raced for 20 years. When I mean Smooth I mean its extremely smooth when warmed up. Like I said tho.. I am starting to question my spark plug gauge for gapping. The factory were all over .050.. if its off then its possible it could be gapped super low. its a tiny gap i know that much.
Take a look at this post
https://www.f150forum.com/f38/anyone...ke-fix-386710/
I would not recommend the top video, but look towards the end posts for links.
Big older post here:
https://www.f150forum.com/f38/drives...es-fix-153099/
#7
Senior Member
When I did my plug change I damaged the electrode on the new plug. I guess I hit it on the way into the cylinder. I re-gapped the plug and all was good. Check each one and make sure you did not do they same.
Hope it helps.
Hope it helps.
Trending Topics
#10
Take a look at this post
https://www.f150forum.com/f38/anyone...ke-fix-386710/
I would not recommend the top video, but look towards the end posts for links.
Big older post here:
https://www.f150forum.com/f38/drives...es-fix-153099/
https://www.f150forum.com/f38/anyone...ke-fix-386710/
I would not recommend the top video, but look towards the end posts for links.
Big older post here:
https://www.f150forum.com/f38/drives...es-fix-153099/