No accelerator pedal response after new motor install
#1
No accelerator pedal response after new motor install
Ok so I changed the motor and tranny and finally got it running today. I have no response at all in the accelerator. It does nothing and occasionally kills the engine when stomped! i hate this fly by wire crap. Any ideas? I did take the little motor off the throttle body as well as the TPS clean and paint eveything and reassembled it. It is a 2006 ford 4 X 4 Roush F150 thanks.
I did search but that left me more confused! The truck sat for almost one year before today but it was always inside
I did search but that left me more confused! The truck sat for almost one year before today but it was always inside
#2
Senior Member
Ok so I changed the motor and tranny and finally got it running today. I have no response at all in the accelerator. It does nothing and occasionally kills the engine when stomped! i hate this fly by wire crap. Any ideas? I did take the little motor off the throttle body as well as the TPS clean and paint eveything and reassembled it. It is a 2006 ford 4 X 4 Roush F150 thanks.
I did search but that left me more confused! The truck sat for almost one year before today but it was always inside
I did search but that left me more confused! The truck sat for almost one year before today but it was always inside
#5
I take it you code for the throttle body and need to replace it ?
#7
I didn't wind it at all! That is probably what I did wrong. I hooked the spring in the groove and put the plastic white piece ontop of it. I think i did it wrong. Why would i replace the throttle body? It's alum!
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#9
If it is coding it is an assembly with its parts. Is your intake hooked up properly? Look to your code now. Is the check engine warning light on ? If the check engine warning light is not on you probably have an air leak somewhere in the air filter intake area unsealed.
Last edited by papa tiger; 01-10-2016 at 10:12 AM.
#10
I will check the codes. I was tired last night when i got it running but it ran too smoothly to have an intake leak. It idled beutifully with headers temps in the low 200's.